Ain't Got No (satisfaction) Fourth Gear
Posted: Thu Aug 04, 2016 11:31 am
So I've done a ton of work on the little bus (my project post is waaay overdue for an update). However one lingering issue (among others, hehe) is that I don't remember ever feeling 4th gear in my auto. This post is possibly a vehicle for a series of condolences which I will also appreciate, however there might be something out there in your collective minds that might just do the trick.
Here's the skinny. Initially I was having issues with a high RPM 3rd gear shift so I performed the following so far.
* Changed the tranny fluid and poured in a can of Seafoam. Ran that for a couple of weeks with some burns up to 80 on the hwy.
* Drained (also drained the torque converter based on another good post).
* When I received the van the 'throttle kickdown linkage' was disconnected (bolt fell out probably). So I reconnected it. It was set to a very narrow setting, like 15mm.
* After reading Gbear's post I tested it at 32mm and had slipping from 1st to second so backed it off again.
* Just before our trip to Carmanah I dropped in a bottle of Rislone trans repair.
* Bus ran fine although trying to drive 100 in 3rd was a stretch at 3,500.
* I've just backed off the linkage even more so I'm probably closer to 25mm gap from 'nub' to cable housing.
* Shifting is happening a bit quicker but still seems to slip from 2nd to 3rd at high revs (need to back off the pedal).
* I've tried to set the 'free play' in the kickdown but I really can't tell what's freeplay and what's worn out plastic linkage.
I recently blanked the EGR so my TPS is moot. I'm just using generic Motomaster ATF.
Bring the condolences. :)
Here's the skinny. Initially I was having issues with a high RPM 3rd gear shift so I performed the following so far.
* Changed the tranny fluid and poured in a can of Seafoam. Ran that for a couple of weeks with some burns up to 80 on the hwy.
* Drained (also drained the torque converter based on another good post).
* When I received the van the 'throttle kickdown linkage' was disconnected (bolt fell out probably). So I reconnected it. It was set to a very narrow setting, like 15mm.
* After reading Gbear's post I tested it at 32mm and had slipping from 1st to second so backed it off again.
* Just before our trip to Carmanah I dropped in a bottle of Rislone trans repair.
* Bus ran fine although trying to drive 100 in 3rd was a stretch at 3,500.
* I've just backed off the linkage even more so I'm probably closer to 25mm gap from 'nub' to cable housing.
* Shifting is happening a bit quicker but still seems to slip from 2nd to 3rd at high revs (need to back off the pedal).
* I've tried to set the 'free play' in the kickdown but I really can't tell what's freeplay and what's worn out plastic linkage.
I recently blanked the EGR so my TPS is moot. I'm just using generic Motomaster ATF.
Bring the condolences. :)